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Project Background
There are three existing 1x630MW supercritical boiler. Before denitration, the NOx concentration is about 400mg/ Nm3, and the design value of low nitrogen +SNCR emission concentration is ≤150mg/ Nm3 (6% oxygen content in dry basis).At present, it is planned to carry out ultra-low emission on the boilers, aiming to reach the NOX emission concentration in the the level of 30~50mg/Nm3 (6% oxygen content in dry basis).

Effluent Standard

Adopt the latest national standard or general international standard
Technical Characteristics

SCR denitration efficiency is 80~ 90%;
When SCR is put into normal operation, the ammonia escape concentration of denitration device is 2.0~2.5 ppm;
When SCR is put into normal operation, the conversion rate of SO2/SO3 is less than 0.75%;
The availability rate of the whole denitration system is more than 98% in one year after the formal handover;
Under the condition of BMCR and the NOx concentration in flue gas: 400mg/Nm3 (standard state, dry basis, 6% oxygen), Party B shall ensure that the urea consumption of each furnace is ≤ 115kg/h (total consumption of SNCR and SCR system).
Solution

Plus SCR on the basis of Low NOx + SNCR


Get The Effect
Make the NOx emission concentration in the reformed flue gas be 30~50mg/Nm3 (6% oxygen in dry basis).